My GMC at Home
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March 2004 Trip to GMCWS Rally - Palm Desert,
CA. Link to the Conclusion (Bottom of page)
February 27: Hoping for a March 7th-ish departure. We'll see how it goes.
February 29: Can't help but wonder if the fan contributed. The reason I say that is that the designs of the fan (serpentine belt setup) is quite different from the original. The blades are not equally spaces and some blades curve sharper at the end. Will be doing a little more research on the subject but I would imagine if the fan was bad it would vibrate a bunch. The new pump. Straight blades so that it is truly bi-directional. The serpentine belt setup runs the pump in a reverse direction. The removed pump. A reverse flow Mondello.
March 1, 2004: Made some inquiries re the fan and all seems well. Will just have to trust GM. March 6, 2004: Test run went well. Even ride-height was pretty close. Upon return I was going to start the Generac to warm it up to ready it for an oil and filter change. It didn't happen. No fuel getting to the GenSet. Of course I left the easiest for last and replaced filters and fuel pump before blaming the GenSet itself. It's just not letting any fuel in. But that's for after breakfast today. The GenSet ProblemI spent yesterday and today chasing and conquering the fuel starved GenSet. After changing filters and checking fuel line I finally came to my senses and disconnected the line going 'to' the GenSet to see if it would draw fuel and sure enough it did. The culprit was the GenSet not taking the fuel it was given. The reason: lack of use. Todays' crappy gas likes to gum things up and that's exactly what happened. Removed the carburetor and cleaned it and lo and behold, it worked after re-installing :-)) So, long story short... I'm going to try and run it once a month. Been meaning to, but have not been good at it in the past. Tomorrows project: chase a non-operating license plate light. Have never been in there since I got the coach. Screws are ceased tight. Probably have to dig at it from inside :-( Still hoping for a Monday departure for a leisurely trip to Palm Desert. March 11, 2004: The trip has not been totally uneventful. Here are some babblings of the sometime/somewhat excitement incurred. March 19, 2004: We dropped down to 38mph in second. Not sure if that's normal or not. Perhaps you could drop an email with your own Grapevine experiences. We did breakfast in the Rest Area at the top, or almost top and then did a little shopping in Valencia before heading east on 210. We started to see a few GMC's. As we neared Pasadena traffic ground to a halt as the freeway was closed at the Pasadena Tunnel. Eventually back on track. Had lunch at the Palm Springs Rest Area so that check-in would be a little easier, or at least with tummies full. Got our spot but found that we'd have to move as it was just for the night. Dave was very helpful to re-arrange our spot so that we might have a chance at latching on to the WiFi at the Clubhouse. This turned out well as Kerry Tandy and his DataStorm weren't able to make it. By putting up a high gain WiFi antenna I as able to connect a bridge to the resorts WiFi and rebroadcast so that at least a few coaches were able to get connected. The rebroadcast turned less efficient as planned. The high gain antenna was for rebroadcast had to be used with bridge instead so we did not cover as many coaches as I had hoped for. Oh well, maybe next time. The plan to get the wireless web cam to the demonstration and vendor sites also went down the proverbial tube as we couldn't get the range. Back to the drawing board. Maybe we'll get another chance in future and put to use what we've learned. Last full day at the Rally today. Planning Bakersfield for Saturday and Sacramento for Sunday. March 21, 2004 March 24, 2004 - Back Home. Departed SAC reasonably early on Monday morning and stopped early at Valley of the Rogue State Park. Very nice place with full hookups at many sites. Early departure saw us deliver the bogie in Tacoma in the late afternoon and got us home at 11PM after waiting out the Seattle rush hour. Long day, but they are always a little easier on the homeward stretch. That's it for this trip. Now for the cleanup and some regular mtce. to have it ready for the next one. A post script regarding my flasher problems early in the trip. It is quite possible that the user contributed when installing new license plate light. Not confirmed, but possible. I don't want the coach to take all the blame when/if there were extenuating circumstances . The conclusion to the March travels Then... as I activated the flashers while waiting for emergency fuel, the user screw-up came into play and blew that fuse. And fuses continued to blow until the cause was removed, which turned out rather simple at the end, i.e. temporarily undo the users doings (disconnect the extended license plate light) . Had I gone a different route to find power for that extended license plate light there probably would not have been any problem but it seemed so simple to use the toad connector. Of course there is a chance now that fuse blowing mysteriously will be a thing of the past, I.e. the destroyed (rusted) original license plate light assembly is no more. The fixing commenced by removing bed and back panel to gain access to the license place light. What I found was plain old yuk. Rusted out lamp assembly and corrosion on the connector. I replaced the lamp assembly with a two-wire type so that there is less reliance on getting the fixture a good ground. Here is how it turned out along with the usual additional problems and solution that always creep in causing any GMC project to expand in scope.
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